EM2019WSP06/Pobleme und offene Punkte
Problems during the development
Despite having enabled the PWM Service of Zephyr there still no PWM Signal in the desired pin. The Solution was editing the
pimux.c file of the board.
To be done
At first the two motors and wheels were very suboptimal and the drive direction was terrible. It got better with the new motors and wheels but still not a straight driving. At the moment only one PWM Signal control the speed of both motors. Adding another PWM Signal and testing again would do an improvement of the straight driving problem.